Tweaking a Safety Planer
Posted: Sun Dec 20, 2020 11:13 am
I was excited to receive a Stewmac safety planer to use on my first attempt at a guitar neck but wasn't too thrilled when I actually went to use it. It was somewhat of a white knuckle experience and I wasn't convinced it was worth the effort. Further investigating with a dial indicator showed the perimeter of the planer was .013 out and a simple application of a sharpie to the spinning planer (cutters removed) confirmed it wasn't the drill press but the threaded arbor hole was not straight.
Stewmac understood my problem and shipped another right away (no return required). They checked one out beforehand an assured me it was less than .004 out total.
Meanwhile, I decided to bore the original to accept a pressed in shaft. I have some machining experience and access to a machine shop so this was not something that would be worth hiring out but the results were like night and day. It seems to work a bit better than the replacement, a quick touch with a sharpie shows it is more accurate.
So if you are having any doubts or problems with a safety planer, it might be worth doing the simple test with a sharpie marker
Stewmac understood my problem and shipped another right away (no return required). They checked one out beforehand an assured me it was less than .004 out total.
Meanwhile, I decided to bore the original to accept a pressed in shaft. I have some machining experience and access to a machine shop so this was not something that would be worth hiring out but the results were like night and day. It seems to work a bit better than the replacement, a quick touch with a sharpie shows it is more accurate.
So if you are having any doubts or problems with a safety planer, it might be worth doing the simple test with a sharpie marker